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Locomotive A3 was built for Coras Iompair Éireann
(CIE), the Irish State owned transport company by Metropolitan
Vickers at their premises at Dukinfield, Manchester, in 1956. A3
was part of a class of 60 Co-Co locomotives, designated “A”
class and numbered A1 – A60 inclusive, which were ordered as
part of the drive to eliminate the majority of steam traction
from the railways of the Irish Republic in the late 1950s. The
contract to build these locomotives was signed at Heuston
Station, Dublin, on 5th May 1954. The bodies for the sixty “A”
class locomotives were constructed by Metropolitan Cammell at
their Midland Works in Birmingham between 1954 and 1956. The
English Steel Corporation constructed the bogies in Sheffield,
and Crossley Brothers at Openshaw, Manchester, supplied the
engines. The electrical equipment for these locomotives was
provided by Metropolitan Vickers Electrical Co. Ltd. The
completed locomotive bodies were then transported by low loader
to Metropolitan Vickers’s premises at Dukinfield, Manchester,
for fitting of their engine/generator sets, bogies and for
testing prior to shipping to Ireland.
A3 eventually entered traffic with
CIE on 27th September 1955, being the first of its type to enter
traffic. When built, these locomotives were originally fitted
with a Crossley HSTV8 engine of 1200 hp. However, the Crossley
engines proved to be extremely troublesome and unreliable. In
1968, the decision was taken to re-engine the whole class with
General Motors 12-645E engines of 1325 hp. A3 itself was re-engined
on 10th March 1971, and subsequently re-numbered A3R.
Eventually, the letter classification system was dropped by CIE,
and the locomotive was renumbered to 003.
In early 1994, the Irish Traction
Group were asked by Iarnród Éireann to nominate three 001 (A)
class locomotives for possible preservation by the Group. The
three locomotives selected by the Group as being in the best
condition at the time were 001, 003 and 039. Locomotive 001 was
subsequently ruled out as it suffered a cracked fuel tank, which
left 003 and 039 as the two locomotives to be preserved by the
Group. 003 was selected by virtue of the fact that it was the
last “A” class locomotive to receive a rewire and a body
overhaul in 1993.
Locomotive 003 was also the last
“A” class locomotive in regular service with Iarnród Éireann,
being officially taken out of traffic on 5th April 1995. During
its final few weeks in service it was based at Limerick Depot,
being used to transfer cement wagons between Limerick and the
nearby cement factory at Castlemungret. This locomotive also had
the honour of hauling the last regular passenger service by a
member of this class, when it operated the 09:50 Limerick to
Ballybrophy and 10:20 Ballybrophy to Limerick services on 1st
April 1995. Its final official working was to transfer wagons
from Castlemungret cement factory to the yard at Limerick on 5th
April 1995. However, this was not the end for 003, as staff at
Limerick kept 003 in working order, using it to perform
occasional shunting duties at Limerick Wagon Works. However, 003
was only running on four traction motors at this time, both the
defective motors being on the same bogie.
Following the “farewell” railtour
utilising locomotive A39 on 23rd September 1995, everybody
thought that this was going to be the last passenger working of
a “A” class in Iarnród Éireann ownership, but this proved to be
incorrect. Just two weeks later, 003 put in a very welcome, if
totally unexpected, appearance on the ITG’s “Flying Pig”
railtour, when it was used to haul the railtour the short
distance between Limerick station to Limerick Check and back on
the section from Limerick to Foynes.
Locomotive 003 was eventually
purchased by the Irish Traction Group on 6th December 1995,
aided by a grant of I£ 10,000 from the Irish Heritage Council.
At this point 003 remained stored at Limerick Depot. As part of
the sale agreement, Iarnród Éireann had agreed to replace the
two defective traction motors. On Saturday 9th March 1996, 003
was hauled to Limerick Junction and back to enable the
locomotive to be turned on the triangle at Limerick Junction so
that the bogie with the defective motors could be positioned
under the overhead gantry crane within the main workshop.
However, following further testing, it was found that a third
motor, on the other bogie, was also defective. Three recently
overhauled traction motors were then sent down from Inchicore
Works to Limerick and were fitted during mid-April 1995. Other
electrical and mechanical work was also carried out on 003 at
the same time to ensure that it was now in full working order
once again.
At around this time, preparations
were being made for the “Inchicore 150” anniversary celebrations
over the weekend of 15th/16th June 1996, to which 003 had been
invited. Locomotive 003 was hauled up from Limerick to North
Wall on Saturday 8th June 1996, and then tripped from North Wall
to Inchicore Works the following morning and placed in Diesel
No. 2 Shop. Work immediately commenced on repainting the
locomotive into “black and tan” livery, and renumbering the
locomotive back to A3R. Repainting was finally finished just a
few hours before the gates at Inchicore Works were opened.
Locomotive A3R was positioned at the head of a display of diesel
locomotives outside Diesel No. 2 Shop for the duration of the
event. Following the Inchicore 150 event, A3R was returned to
Limerick for storage on 8th July 1996, where it as to remain for
the next two years or so. Locomotive A3R did venture out briefly
once during this period when it was exhibited at Thurles station
on 6th April 1998.
Following the securing of the
necessary insurance cover to enable the Irish Traction Group to
operate its locomotives under their own power on Iarnród Éireann
tracks, A3R was hauled up from Limerick to Inchicore Works over
the weekend of 18th/19th December 1999 to have its CAWS and
train radio equipment refitted and for it to be certified fit
for main line running. This work was completed on 1st March
1999, and the locomotive was certified fit the following day.
Its first booked passenger working was due to be on the “Back in
Black” railtour on Saturday 27th March 1999. Its first run under
its own power on Iarnród Éireann tracks under ITG ownership was
on 23rd March 1999, when it ran light engine to Kildare and
back. Even this run was delayed by two hours after the fuel pump
burnt out just before the locomotive was due to leave Inchicore
Depot, and had to be replaced with one recovered from spares
donor locomotive 015.
A second loaded test run took
place on 25th March 1996, when A3R hauled a rake of steam vans
and Cravens coaches to Lisduff and back. All went well on the
outward journey, but A3R started to suffer from a loss of vacuum
on the return journey, and a fault also developed with the train
radio. Unfortunately, the faults could not be repaired in time
for the railtour on 27th March 1996, and so locomotive A39 was
used in its place. Following repairs, A3R undertook another
loaded test run to Portlaoise and back on 17th May 1999, in
preparation for its next booked appearance on the “Mayo
Metro-Vick” railtour on Saturday 12th June 1999.
On Friday 11th June 1999
locomotive A3R ran light engine from Inchicore Depot to Dublin
Connolly ready to work the following railtour:
12th June 1999
Mayo Metro-Vick Railtour
A3R operated faultlessly on the
day, working the train from Dublin Connolly to Ballina and back,
the locomotive putting in an impressive, if somewhat “smoky”
performance. A3R returned to Inchicore Depot light engine two
days later.
Locomotive A3R’s next scheduled
appearance was to be on Saturday 9th October 1999, operating the
“Leitrim Leprechaun” railtour from Dublin Connolly to Dromod,
and back to Bray. However, a few days before the railtour,
locomotive A3R developed a serious vibration problem with its
cooling fan, which prevented it being used. A replacement
cooling fan motor was fitted on 9th November 1999, but this did
not rectify the vibration problem. At this point the ITG had
decided not to renew its main line insurance cover due to the
excessive cost and dwindling passenger numbers, and so the
repair work to A3R was put on hold indefinitely.
Between 2000 and 2008 the
locomotive remained stored out of use at Inchicore Works, with
very little work being carried out on it except to try to
protecting it from the elements. However, following the
completion of restoration work on A39 in early 2009, work
restarted on A3R in order to try to return locomotive to working
order once again.
Firstly, the old batteries had to
be removed and safely disposed of as they were no longer fit for
purpose. Over the next few weeks, replacement batteries were
acquired and fitted, and the brushes,
brush arms and commutators in the main and auxiliary generators
were also checked. Some of the starting contactors had to be
replaced as they were found to be sticking. The engine was also
barred over and was found to be relatively free, it having been
several months since it had last been done. The tarpaulin that
had been covering the locomotive was removed, as was the plastic
sheeting that was placed over the exhaust ports when the engine
was drained down in November 1999 which, as it turned out, had
done its job well. The locomotive’s cooling system was filled
and the fuel tank treated with biocide. Oil was also poured over
the top of the cylinder heads, camshafts and injectors inside
the cam boxes.
On Saturday 9th
May 2009 the engine in locomotive A3R was successfully started
for the first time since November 1999. However a faulty battery
caused A3R to be shut down after a short period. Once the
defective battery had been replaced, locomotive A3R was then
restarted, and all was found to be well.
After a couple of hours the
engine sounded quite smooth while it was running, and the smoke
that it was giving off when it first started had disappeared.
The auxiliary generator appeared to be also charging the
batteries correctly.
As the locomotive had been out in the open for several years,
the traction motors would no doubt have been rather damp, so no
attempt was made to move the locomotive under its own power
until further work had been carried out. However, the air system
was found to be working as it should, although one horn valve
and one wiper motor were found not to be working, both on the
second man’s side in No. 1 cab. The heaters in both cabs were
operating correctly, as were the headlights and marker lights at
both ends. The hot plate in No. 1 cab was working, but not the
one in No. 2 cab. The bulb in the cab light was blown in No. 1
cab, otherwise the only non-functioning lights were those
located next to the fuel fillers. All these faults were repaired
over the following couple of weeks.
When the
locomotive’s engine was first filled with coolant, a leak was
found on the water pump that is bolted onto the engine, and was
particularly bad when the engine was cold. The water was
subsequently drained out of the cooling system and the water
pump dismantled. In
mid-June 2009, the water pump was repaired and the pump
re-assembled using new seals. The water pump was then reattached
to the engine and all the water pipes reconnected. The water
system was refilled and the engine barred over. On 20th
June 2009, the engine was restarted and allowed to run for
around three hours to help recharge the batteries. However, it
was not possible to allow the engine to run any longer as the
cooling fan motor fuse had been temporarily removed pending
repairs to the defective fan motor.
In July 2009, the fan blade was
removed from the cooling fan motor in an attempt to find out the
reason for the excessive vibration that resulted in A3R being
“stopped” back in 1999. Once the blade was off, an attempt to
turn the fan motor by hand was made, but it was found to be very
stiff, when it should have rotated very easily. The bearings on
the fan motor were greased and the fuse replaced so that an
attempt could be made to test the motor properly. The fan
started turning when it was first switched on, but rapidly
stopped once the power was switched off. However, after a few
more attempts the fan motor freed up and eventually started to
rotate quite freely. The fan blade was then refitted to the
motor and the protective grill replaced. The fan was then tested
once again, and seemed to revolve well enough without any
rattles and bangs. However, the cooling fan motor does not
appear to be kicking-in at the correct speeds as the engine
temperature rises. Further examination of the wiring in the fan
motor control box still needs to be carried out, and also to the
thermostats that control the fan speed.
The locomotive is now being
started on a regular basis to help keep the batteries fully
charged.
Locomotive A3R was moved by low-loader from Inchicore Works to
the West Clare Railway, Moyasta, Co. Clare, on 23rd
November 2009 for eventual display inside a new museum that is
due to be constructed there in 2010.
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003 Howth Jn 20 May 1989.
Jonathan Allen


A3R in the running shed at
Inchicore. Peter Jones.

A3R being
started for the first time in just under 10 years on 9th
May 2009.
Photo: Aidan
Kehoe |