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Locomotive A3 was built
for Coras Iompair Éireann (CIE), the Irish State owned transport
company by Metropolitan Vickers at their premises at Dukinfield,
Manchester, in 1956. A3 was part of a class of 60 Co-Co
locomotives, designated “A” class and numbered A1 – A60
inclusive, which were ordered as part of the drive to eliminate
the majority of steam traction from the railways of the Irish
Republic in the late 1950s. The contract to build these
locomotives was signed at Heuston Station, Dublin, on 5th
May 1954. The bodies for the sixty “A” class locomotives
were constructed by Metropolitan Cammell at their Midland Works
in Birmingham between 1954 and 1956. The English Steel
Corporation constructed the bogies in Sheffield, and Crossley
Brothers at Openshaw, Manchester, supplied the engines. The
electrical equipment for these locomotives was provided by
Metropolitan Vickers Electrical Co. Ltd. The completed
locomotive bodies were then transported by low loader to
Metropolitan Vickers’s premises at Dukinfield, Manchester, for
fitting of their engine/generator sets, bogies and for testing
prior to shipping to Ireland.
A3 eventually entered
traffic with CIE on 27th September 1955, being the first of its
type to enter traffic. When built, these locomotives were
originally fitted with a Crossley HSTV8 engine of 1200 hp.
However, the Crossley engines proved to be extremely troublesome
and unreliable. In 1968, the decision was taken to re-engine
the whole class with General Motors 12-645E engines of 1325 hp.
A3 itself was re-engined on 10th March 1971, and subsequently
re-numbered A3R. Eventually, the letter classification system
was dropped by CIE, and the locomotive was renumbered to 003.
In early 1994, the Irish
Traction Group were asked by Iarnród Éireann to nominate three
001 (A) class locomotives for possible preservation by the
Group. The three locomotives selected by the Group as being in
the best condition at the time were 001, 003 and 039. Locomotive
001 was subsequently ruled out as it suffered a cracked fuel
tank, which left 003 and 039 as the two locomotives to be
preserved by the Group. 003 was selected by virtue of the fact
that it was the last “A” class locomotive to receive a rewire
and a body overhaul in 1993.
Locomotive 003 was also
the last “A” class locomotive in regular service with Iarnród
Éireann, being officially taken out of traffic on 5th April
1995. During its final few weeks in service it was based at
Limerick Depot, being used to transfer cement wagons between
Limerick and the nearby cement factory at Castlemungret. This
locomotive also had the honour of hauling the last regular
passenger service by a member of this class, when it operated
the 09:50 Limerick to Ballybrophy and 10:20 Ballybrophy to
Limerick services on 1st April 1995. Its final official working
was to transfer wagons from Castlemungret cement factory to the
yard at Limerick on 5th April 1995. However, this was not the
end for 003, as staff at Limerick kept 003 in working order,
using it to perform occasional shunting duties at Limerick Wagon
Works. However, 003 was only running on four traction motors at
this time, both the defective motors being on the same bogie.
Following the “farewell”
railtour utilising locomotive A39 on 23rd September 1995,
everybody thought that this was going to be the last passenger
working of a “A” class in Iarnród Éireann ownership, but this
proved to be incorrect. Just two weeks later, 003 put in a very
welcome, if totally unexpected, appearance on the ITG’s “Flying
Pig” railtour, when it was used to haul the railtour the short
distance between Limerick station to Limerick Check and back on
the section from Limerick to Foynes.
Locomotive 003 was
eventually purchased by the Irish Traction Group on 6th December
1995, aided by a grant of I£ 10,000 from the Irish Heritage
Council. At this point 003 remained stored at Limerick Depot. As
part of the sale agreement, Iarnród Éireann had agreed to
replace the two defective traction motors. On Saturday 9th March
1996, 003 was hauled to Limerick Junction and back to enable the
locomotive to be turned on the triangle at Limerick Junction so
that the bogie with the defective motors could be positioned
under the overhead gantry crane within the main workshop.
However, following further testing, it was found that a third
motor, on the other bogie, was also defective. Three recently
overhauled traction motors were then sent down from Inchicore
Works to Limerick and were fitted during mid-April 1995. Other
electrical and mechanical work was also carried out on 003 at
the same time to ensure that it was now in full working order
once again.
At around this time,
preparations were being made for the “Inchicore 150” anniversary
celebrations over the weekend of 15th/16th June 1996, to which
003 had been invited. Locomotive 003 was hauled up from Limerick
to North Wall on Saturday 8th June 1996, and then tripped from
North Wall to Inchicore Works the following morning and placed
in Diesel No. 2 Shop. Work immediately commenced on repainting
the locomotive into “black and tan” livery, and renumbering the
locomotive back to A3R. Repainting was finally finished just a
few hours before the gates at Inchicore Works were opened.
Locomotive A3R was positioned at the head of a display of diesel
locomotives outside Diesel No. 2 Shop for the duration of the
event. Following the Inchicore 150 event, A3R was returned to
Limerick for storage on 8th July 1996, where it as to remain for
the next two years or so. Locomotive A3R did venture out briefly
once during this period when it was exhibited at Thurles station
on 6th April 1998.
Following the securing of
the necessary insurance cover to enable the Irish Traction Group
to operate its locomotives under their own power on Iarnród
Éireann tracks, A3R was hauled up from Limerick to Inchicore
Works over the weekend of 18th/19th December 1998 to have its
CAWS and train radio equipment refitted and for it to be
certified fit for main line running. This work was completed on
1st March 1999, and the locomotive was certified fit the
following day. Its first booked passenger working was due to be
on the “Back in Black” railtour on Saturday 27th March 1999. Its
first run under its own power on Iarnród Éireann tracks under
ITG ownership was on 23rd March 1999, when it ran light engine
to Kildare and back. Even this run was delayed by two hours
after the fuel pump burnt out just before the locomotive was due
to leave Inchicore Depot, and had to be replaced with one
recovered from spares donor locomotive 015.
A second loaded test run
took place on 25th March 1999, when A3R hauled a rake of steam
vans and Cravens coaches to Lisduff and back. All went well on
the outward journey, but A3R started to suffer from a loss of
vacuum on the return journey, and a fault also developed with
the train radio. Unfortunately, the faults could not be repaired
in time for the railtour on 27th March 1999, and so locomotive
A39 was used in its place. Following repairs, A3R undertook
another loaded test run to Portlaoise and back on 17th May 1999,
in preparation for its next booked appearance on the “Mayo
Metro-Vick” railtour on Saturday 12th June 1999.
On Friday 11th June 1999
locomotive A3R ran light engine from Inchicore Depot to Dublin
Connolly ready to work the following railtour:
12th June 1999
Mayo Metro-Vick Railtour
A3R operated faultlessly
on the day, working the train from Dublin Connolly to Ballina
and back, the locomotive putting in an impressive, if somewhat
“smoky” performance. A3R returned to Inchicore Depot light
engine two days later.
Locomotive A3R’s next
scheduled appearance was to be on Saturday 9th October 1999,
operating the “Leitrim Leprechaun” railtour from Dublin Connolly
to Dromod, and back to Bray. However, a few days before the
railtour, locomotive A3R developed a serious vibration problem
with its cooling fan, which prevented it being used. A
replacement cooling fan motor was fitted on 9th November 1999,
but this did not rectify the vibration problem. At this point
the ITG had decided not to renew its main line insurance cover
due to the excessive cost and dwindling passenger numbers, and
so the repair work to A3R was put on hold indefinitely.
Between 2000 and 2008 the
locomotive remained stored out of use at Inchicore Works, with
very little work being carried out on it except to try to
protecting it from the elements. However, following the
completion of restoration work on A39 in early 2009, work
restarted on A3R in order to try to return locomotive to working
order once again.
Firstly, the old batteries
had to be removed and safely disposed of as they were no longer
fit for purpose. Over the next few weeks, replacement batteries
were acquired and fitted, and the brushes,
brush arms and commutators in the main and auxiliary generators
were also checked. Some of the starting contactors had to be
replaced as they were found to be sticking. The engine was also
barred over and was found to be relatively free, it having been
several months since it had last been done. The tarpaulin that
had been covering the locomotive was removed, as was the plastic
sheeting that was placed over the exhaust ports when the engine
was drained down in November 1999 which, as it turned out, had
done its job well. The locomotive’s cooling system was filled
and the fuel tank treated with biocide. Oil was also poured over
the top of the cylinder heads, camshafts and injectors inside
the cam boxes.
On Saturday 9th May 2009 the engine in locomotive A3R
was successfully started for the first time since November 1999.
However a faulty battery caused A3R to be shut down after a
short period. Once the defective battery had been replaced,
locomotive A3R was then restarted, and all was found to be well.
After a couple of hours the
engine sounded quite smooth while it was running, and the smoke
that it was giving off when it first started had disappeared.
The auxiliary generator appeared to be also charging the
batteries correctly.
As the locomotive had been out in the open for several years,
the traction motors would no doubt have been rather damp, so no
attempt was made to move the locomotive under its own power
until further work had been carried out. However, the air system
was found to be working as it should, although one horn valve
and one wiper motor were found not to be working, both on the
second man’s side in No. 1 cab. The heaters in both cabs were
operating correctly, as were the headlights and marker lights at
both ends. The hot plate in No. 1 cab was working, but not the
one in No. 2 cab. The bulb in the cab light was blown in No. 1
cab, otherwise the only non-functioning lights were those
located next to the fuel fillers. All these faults were repaired
over the following couple of weeks.
When the locomotive’s engine was first filled with coolant, a
leak was found on the water pump that is bolted onto the engine,
and was particularly bad when the engine was cold. The water was
subsequently drained out of the cooling system and the water
pump dismantled.
In mid-June 2009, the water pump was
repaired and the pump re-assembled using new seals. The water
pump was then reattached to the engine and all the water pipes
reconnected. The water system was refilled and the engine barred
over. On 20th June 2009, the engine was restarted and
allowed to run for around three hours to help recharge the
batteries. However, it was not possible to allow the engine to
run any longer as the cooling fan motor fuse had been
temporarily removed pending repairs to the defective fan motor.
In July 2009, the fan
blade was removed from the cooling fan motor in an attempt to
find out the reason for the excessive vibration that resulted in
A3R being “stopped” back in 1999. Once the blade was off, an
attempt to turn the fan motor by hand was made, but it was found
to be very stiff, when it should have rotated very easily. The
bearings on the fan motor were greased and the fuse replaced so
that an attempt could be made to test the motor properly. The
fan started turning when it was first switched on, but rapidly
stopped once the power was switched off. However, after a few
more attempts the fan motor freed up and eventually started to
rotate quite freely. The fan blade was then refitted to the
motor and the protective grill replaced. The fan was then tested
once again, and seemed to revolve well enough without any
rattles and bangs. However, the cooling fan motor does not
appear to be kicking-in at the correct speeds as the engine
temperature rises. Further examination of the wiring in the fan
motor control box still needs to be carried out, and also to the
thermostats that control the fan speed. However, with the need
to remove this locomotive from Inchicore works, Dublin, by the
end of November 2009, work on returning locomotive A3R to full
working order was halted for the foreseeable future.
Locomotive A3R was moved
by low-loader from Inchicore Works, Dublin, to the West Clare
Railway, Moyasta, Co. Clare, at the end of November 2009 for
display in a museum that is due to be constructed at the site.
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003 Howth Jn 20 May 1989.
Jonathan Allen


A3R in the running shed at
Inchicore. Peter Jones.

A3R being
started for the first time in just under 10 years on 9th
May 2009.
Photo: Aidan
Kehoe |