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This was the first main line
diesel locomotive to be preserved in Ireland, being handed over
to the ITG on 23rd October 1992. No. 226 was
eventually moved down to Carrick-On-Suir in December 1992. Over
the next couple of years good progress was then made on
stripping down the locomotive ready for overhaul and
restoration.
However, in early 1996, work on
No. 226 virtually ground to a halt. Around this time, three of
the Group’s other locomotives that were also stored at
Carrick-On-Suir, Nos. 231, G601 and G611, were all moved to
Inchicore Works for display at the proposed open weekend to
celebrate the 150th anniversary of the Works in June
1996. Unfortunately, the extra work required to prepare these
locomotives for display diverted attention away from No. 226 for
several months. All three of these locomotives needed repainting
prior to display, along with 001 (A) class locomotive No. A3R,
which was already at the Works. In addition to the repainting
work, locomotive No. 231 also required extensive re-panelling
work to be done to the cabs and body sides.
Over the next couple of years,
faced with the constant attack from vandals at the Carrick-On-Suir
site, coupled with other increasing family commitments of those
who worked there, little work was done on No. 226. The
subsequent main line operation of our two 001 (A) class
locomotives in 1999/2000 also kept our small band of volunteers
away from Carrick-On-Suir and No. 226. Furthermore, at around
this time, the Group’s other 201 (C) class locomotive No. C231
had just been moved back to the UK for restoration, which meant
that restoration work on No. 226 was now low down on our list of
priorities.
However, in 2003, one of our most active and enthusiastic
members, Aidan Brosnan, moved down to Clonmel and resumed work
on No. 226. To date, significant progress has been made on the
restoration of No. 226.
Cab No. 2
This cab was completely stripped
out to enable the rotten cab floor to be replaced. The areas
under the driver’s and secondman’s desks were the worst
affected, having completely rotted through in several places.
Corrosion had also affected the supports for the desks
themselves. New sections of flooring were welded into position
and the desks repaired. In addition, new cab side panels have
been welded into position to replace the original panels which
were also badly corroded. A new headlamp box was welded to the
cab roof, as the original box had almost completely rusted away.
New felt lined channels and “jumping-jack” springs have been
fitted to the cab droplight windows. All the timber frames that
surround the cab doors and windows have been replaced and
repainted. Repainting of
the underside of the cab floor has also been completed. Mastic
has now been applied under the floor of the cab to prevent water
lodging between the floor and the main girders. Furthermore,
mastic has also been applied inside the cab behind the desks to
stop corrosion between the cab outer panels and the supporting
frame.
Once all the bodywork repairs
were completed, work commenced on re-assembling the cab. Every
single component that was removed from this cab has been cleaned
up and repainted. The wooden supports for the cab floor have
been replaced or renewed, and new trunking to carry the
electrical control cables under the cab floor has also been
welded into position. All
of the remaining control air pipes have been re-fitted into the
cab, along with the windscreen wiper valves and a horn valve.
Two new vacuum hoses to connect the vacuum brake valve to the
train pipe were also fitted.
The driver’s and secondman’s
desks, together with the central control console, have been
completely rebuilt, and new desk tops fitted.
The five electrical terminal
boards that fit inside the centre section of the driver’s desk
have been replaced, along with the cab hotplate. A replacement
de-mister element has been tested and fitted.
All the electrical conduits have
been cleaned up, repainted and replaced. All air pipes have been
pressure tested to check for leaks. The air and vacuum brake
valves inside the central control console have been overhauled
and tested. The power controllers have been cleaned up, together
with all the electrical finger contacts, and refitted back into
the desks. The cab heaters have been overhauled and refitted.
Both cab seats were completely stripped down, cleaned up and
rebuilt. The cab and engine room doors have also been repainted
internally and their locking mechanisms repaired.
New neoprene sponge seals have
also been fitted around the cab doors.
A set of marker light switches
have been re-fitted to the bulkhead above the engine room door.
The two
deadmans’ pedals have been cleaned out and repainted. The foot
heating elements have also been refitted back under the desks.
The box that houses the
switches and warning indicator lamps has been cleaned out. The
vigilance box has been replaced on the bulkhead. The “Low Oil
Pressure” and “Vigilance” lamps have been refitted to their
plate and their labels have been repainted. The two baggage
racks have been repainted and refitted. The ammeters have also
been cleaned up.
The
re-assembly and rewiring of the cab has now been completed.
All the various switches, earth fault and overload alarm and
reset, the hot engine alarm, low oil pressure indicator and
the starting contactor circuits have been successfully
tested. A new plywood floor has now also been fitted into
the cab. The only work required to complete the restoration
of the cab is to replace the original windscreens with new
laminated windscreens, replace the inspection covers on the
control desk, and re-fit the cab seats and handbrake
pedestal.
Cab No.1
Cab No.1 cab was originally kept
intact as a reference of how to reassemble cab No. 2. However,
once No. 2 cab had been reassembled, work commenced in 2006 in
stripping out No. 1 cab. Just like No. 2 cab, certain areas of
the cab floor had rotted away, however the damage was found to
be a lot less severe. In order to carry out the necessary
repairs, both power controllers and desk corners have been
removed to gain access to the affected areas. The rotten
steelwork has been cut out, and the holes squared up ready for
new steel plate to be welded into position. One cab side panel
has so far been replaced. It is intended that this cab will be
completely rebuilt to the same standard as Cab No. 2.
Engine
Room and Cooler Group
All of the steel framework that
supports the roof panels and the cooling fan assembly have been
cleaned up, repainted, and refitted back into the locomotive.
All the engine room cable
trunking has been cleaned out and repainted. In addition, 40
years’ worth of accumulated thick oil, muck and grease has been
scraped out from around the engine tray. The engine room floor
has been completely cleaned of all oil and grease, and has now
been repainted. The engine room walls have been completely
repainted, and all of the internal air pipes and cable conduit
have now been replaced. The
Duplex Check Valve and the Reducing Valve on the control air
circuit have been set to their correct operating pressures. The
traction motor blower housing, and the rear fan cover plate have
been cleaned down and repainted. The engine compartment lamps
were rewired and successfully tested on 18th November
2006. This is the first time the lamps have worked in over 22
years.
The
vertical supports for the cooler group header tanks were
cleaned down and repainted. The cooler group header tanks
themselves were sent away to a specialist engineering
company in order to have their faces machined. This was done
in order to ensure a water tight seal once the radiator
elements were replaced. The faces were found to be generally
straight, but some of them were badly pitted by rust. The
machining operation obtained a “like new” surface finish
along the faces of the header tanks. Meanwhile, the 40
radiator elements were sent away to another specialist
contractor for cleaning, pressure testing and flow testing.
120 new studs were obtained in order to re-attach the
radiator elements to the header tanks. New cork gaskets were
glued onto the edges of the header tanks where they touch
the locomotive’s body.
Re-assembly of the first radiator bank was eventually
completed in February 2008. Re-assembly of the second
radiator bank was started in June 2008. Once completed, both
radiator banks will then be pressure tested. Meanwhile, all
the surrounding ducting has been cleaned up and repainted.
This will be refitted once the pressure testing of the
radiator banks has been completed.
Some years ago, a major defect
was discovered on the power unit. A small section of the engine
block, where the cam shaft was attached, had cracked and broken
loose due to excessive vibration on the cam shaft. This broken
piece was welded back into place. The effectiveness of this
repair will only be determined when the engine is started up. A
replacement power unit from a 141/181 class locomotive may have
to be obtained in due course.
Low and High
Tension Cubicles
Both
electrical control cubicles were completely stripped out to
enable the electrical control equipment to be overhauled,
and for the insides of the cubicles to be cleaned out and
repainted. All the inspection panels that fit on the engine
room side of the electrical control cubicles have been
repainted and new neoprene foam seals applied to the edges
of the panels.
The
interlock contacts for the main generator field contactor
have been cleaned up and refitted inside the low tension
cubicle. All seven of the auxiliary contactors have been
completely reconditioned, tested and refitted. All of the
thick cables and copper straps have also been replaced. Both
of No. 226’s starting contactors have been overhauled and
refitted back into the high tension cubicle. Both traction
motor overload panels have been reconditioned and refitted.
The starting relay and traction motor isolator have been
overhauled and replaced inside the high tension cubicle. The
traction motor field divert switch unit has been cleaned
down and refitted. All of the circuit breakers have been
tested and refitted to the fuse and circuit breaker panel,
which has then been refitted into the low tension cubicle.
The battery isolating switch and voltage regulator have been
cleaned up and refitted back into the low tension cubicle.
The
reverser was stripped down, cleaned up, checked over,
re-assembled and then refitted back into the high tension
cubicle. The air valves on the reverser had to be replaced
as the original ones were found to be leaking. Following
this, an air supply and 110 volt DC supply were connected to
No. 226. The reverser was then checked using the
forward/reverse handles in No. 2 cab and was found to be
working correctly. All of the cables for the traction motors
have been fed into the high tension cubicle and connected to
the reverser whilst the other ends have been laid out down
the trunking in the engine room floor.
A
replacement bracket to support the main ammeter shunt
resistor was fitted, followed by the main ammeter shunt
resistor and the main generator cables. All of the control
cables were fitted and wired to the main terminal board.
The four
traction motor switches were inspected and repaired where
necessary. The insulating bars were touched up with
anti-tracking paint and the contact tips were cleaned up and
replaced with new ones where necessary. Following the
replacement of the four motor switches, the control cables
were connected and the air pipes were attached. The motor
switches were then successfully open and closed as forward
and reverse were selected. In addition, a more permanent
connection for a 110 volt shore supply to power the engine
room lamps was fitted to the low tension cubicle.
The rewire
and replacement of components in both the high tension
cubicle and low tension cubicle has now been completed.
General
The battery boxes have also been
cleaned out and the paintwork touched up. A
section of battery cable conduit was replaced between the two
battery boxes. The cable between the two boxes was then
replaced, with some difficulty, through the conduit.
A battery charging socket
and interlock unit have been replaced and the wires fed into the
low tension cubicle.
Both engine compartment bulkhead
doors have been fully repainted and their handles and locking
mechanisms refitted. Two lamp irons for the No. 1 end buffer
beam have been repaired. Four marker lamp boxes have been fully
reconditioned and reassembled. New cables have also been fitted,
as well as the rubber gasket which fits between the lamp box and
the locomotive body.
The main reservoir
equaliser and the independent equaliser pipes, which go through
the buffer beam at the No. 2 end, have been refitted on the
second man’s side. A
section of control air pipe that goes through the buffer beam at
No. 2 end has also been re-fitted. New rubber seals and gaskets
for the air brake valves have been purchased from Metcalfe’s,
who originally manufactured the brake valves for the locomotive.
These will be used to overhaul the brake valve for No. 1 end,
and also to refurbish a spare valve. Rubber gaskets have also
been obtained from the same company for the mounting of the
triple valve.
A spare
fuel pump motor has been overhauled by a specialist
contractor. A good fuel pump was fitted to it upon its
return and the complete unit was then painted and refitted
underneath the locomotive.
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